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    埋地输气管道的腐蚀数据浅析

    Brief Analysis on Corrosion Data of Buried Gas Transmission Pipeline

    • 摘要: 以某城市埋地输气管线为研究对象,结合杂散电流干扰及治理的情况,对全线阴保桩测试数据以及开挖结果进行分析。结果表明:通过调整恒电位仪并进行极性排流等措施,欠保护率明显下降,过保护率大幅度上升,全线管道阴极保护有效;近期交流电流密度呈现增大趋势是由于附近新增2处干扰源。根据阴保监测数据及开挖验证结果,初步判断2处腐蚀坑是由于直流杂散电流干扰。分析管道的腐蚀数据可以更有效地指导管线的腐蚀监测与防护,为保证全线管道的有效运行,需要更深入挖掘数据。

       

      Abstract: Taking a buried gas pipeline in a certain city as the research subject, the test data of cathodic protection (CP) test stations and excavation results along the entire pipeline were analyzed, in combination with stray current interference and mitigation measures. The results show that by adjusting the potentiostat and implementing measures such as polarity drainage, the under-protection rate of the pipeline significantly decreased, while the over-protection rate notably increased, indicating effective cathodic protection across the entire pipeline. The recent increase in AC current density was attributed to two newly added interference sources nearby. Based on drainage protection monitoring data and excavation verification, it was preliminarily determined that two corrosion pits were caused by DC stray current interference. Analyzing pipeline corrosion data could more effectively guide corrosion monitoring and protection efforts. To ensure the efficient operation of the entire pipeline, further in-depth data analysis was required.

       

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